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reduction ratio相关的网络例句

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与 reduction ratio 相关的网络例句 [注:此内容来源于网络,仅供参考]

Studied the solid particles cyclone separation under structural parameters and operating parameters of different hydrocyclone, the results showed that major factor influence split ratio is in the ratio of entrance to exit pressure of hydrocyclone. Exit pressure has a certain influence on the split ratio, the various of the diameter and cone angle of hydrocyclone (in the ratio of entrance to exit pressure is constant) have no influence on split ratio; With diameter and cone angle increase, the separation granularity gradually increasing and recovery ratio decreasing; With entrance pressure increase, the separation granularity of hydrocyclone decrease, the split ratio of underset will increase slowly; With the diameter of overflow pipe increase, the separation granularity of hydrocyclone increasing and recovery ratio decreasing; With the diameter of underset pipe increasing, the separation granularity of hydrocyclone decreasing and recovery ratio increasing.

在不同的水力旋流器结构参数和操作参数下,对固体颗粒的旋流分离进行了分析研究,结果表明:旋流器的排出口比是影响分流比的主要因素,进口压力对分流比有一定影响,水力旋流器的直径变化和锥段角度变化对分流比基本上没有影响;随着直径、锥段角度的增大,分离粒度逐渐增大,回收率降低;随着入口压力增大,水力旋流器的分离粒度变小,底流的分流比会缓慢增加;随着溢流管管径的增加,分离粒度增大,分流比明显减小,回收率降低;随着底流管直径的增加,分离粒度减小,分级效果明显下降,回收率会增加。

With the raw material and the particle size of reducing agent narrowed, the percent reduction of strontia increases.(6) With the barbecuing pressure increasing, the percent reduction of strontia increases, after the certain value, the percent reduction of strontia decreases instead.(7) With reduction temperature increasing, the percent reduction of strontia increases.(8) The percent reduction of strontia is increasing with prolonging reduction time. In this experimental condition, it will become steady after 2.5h.

通过实验研究确定以SrCl_2-SrF_2-SrCO_3的纯锶盐体系作为电解质,实验中还采用了我们最新研制的熔盐电解监控仪对电解过程进行测量和系统的研究,得出以下结论:(1)增加电流强度,反电动势亦随之增加,而升高温度反电动势则有所降低;(2)随着电流密度的升高和电解时间的延长,电流效率逐渐增加,达到峰值后稳步下降;(3)延长电解时间,合金中锶的含量逐渐增加,最高可达18.1%;(4)开始电解后,反电动势逐渐增加,但向熔体中加入SrCO_3后,反电动势明显降低,因此认为在正常电解时是SrCO_3在分解。

In the paper,the transmission of designed roller oscillating tooth reduction gear adopts osci llating tooth gear drive without exception,one-stage reduction gear and two-stage reduction gear have joined through spline coupling band;The joining way of shock wave thellomble and oscillating tooth adopts the biserial bearing of without inner ring of needle bearing,and directly adopts bearing outer ring as shock wave thellomble;Center wheel of two-stage reduction gear and center wheel of two-stage reduction gear passes through taper thread,and center wheel is fixed;As soon as the flange of input end and center wheel of one-stage reduction gear,the flange of export end and center wheel of two-stage reduction gear makes monobloc structure.

本文预设的井下减速器的传动均采用活齿传动,一级减速器的输出轴和二级减速器的输入轴通过花键联轴套联接;激波环与活齿的毗连方式采用能蒙受较大载荷的无内圈双列滚针不锈钢管,且直接采用不锈钢管外圈作为激波环;一级减速器的中心轮和二级减速器的中心轮是通过锥螺纹毗连的,且中心轮固定;一级减速器的中心轮与输入端的法兰盘,二级减速器的中心轮与输出端的法兰盘均做成整体的结构。

In the paper,the transmission of designed roller oscillating tooth reduction gear adopts oscillating tooth gear drive without exception,one-stage reduction gear and two-stage reduction gear have joined through spline coupling band;The joining way of shock wave thimble and oscillating tooth adopts the biserial bearing of without inner ring of needle bearing,and directly adopts bearing outer ring as shock wave thimble;Center wheel of two-stage reduction gear and center wheel of two-stage reduction gear passes through taper thread,and center wheel is fixed;As soon as the flange of input end and center wheel of one-stage reduction gear,the flange of export end and center wheel of two-stage reduction gear makes monobloc structure.

本文设计的井下减速器的传动均采用活齿传动,一级减速器的输出轴和二级减速器的输入轴通过花键联轴套联接;激波环与活齿的连接方式采用能承受较大载荷的无内圈双列滚针中国财经圈,中国财经圈,且直接采用进口中国财经圈外圈作为激波环;一级减速器的中心轮和二级减速器的中心轮是通过锥螺纹连接的,且中心轮固定;一级减速器的中心轮与输入端的法兰盘,二级减速器的中心轮与输出端的法兰盘均做成整体的结构。

The experiment and the research indicate that:(1) Through the Hot-Continuous-Rolling production technics under small reduction ratio of 4.04 and 5.08, the rectangular continuous-casting billet of 235×265mm can be used to produce big size steel stick of Φ140mm and Φ 125mm whose macrostructure and mechanical properties meet the standards, this technics is viable;(2) This rolling technics can make the deformation penetrate to the center of the billet by low temperture and low velocity and big roller diameter and large reduction quantity at every pass and optimum design and arrangement of rollers, which is the key of Hot-Continuous-Rolling technics under small reduction ratio;(3) The sending technics used in Xining Special Steel Co.,Ltd can not use waste-heat of billet adequately, but the sensitive temperature section of A1N or sulphides or inclusions separating out is avoided, creating a favorablecondition for insuring good surface quality of final rolled steel;(4) The Hot-Continuous-Rolling technics under small reduction ratio has a close relationship with the billet quality control and the hot sending process control and the cooling control after rolling.

通过实验研究表明:(1) 235×265mm矩形连铸坯分别采用4.04和5.08的小压缩比热连轧生产工艺,所生产的Φ140mm和Φ125mm的大规格棒材,其低倍组织和机械性能均符合标准要求,该工艺是可行的;(2)本实验所采取的低温低速、大辊径大道次压下量轧制工艺加上轧辊孔型的优化设计与配置,可以使加工变形渗透到铸坯的中心,这一点是实现小压缩比热连轧生产工艺的关键;(3)西宁特钢在红送过程中虽然铸坯余热未能得到充分的利用,但是有效地避开了A1N、硫化物的析出及夹杂物偏析的敏感温度区,为保证最终轧材良好的表面质量创造了有利的条件;(4)小压缩比热连轧生产与铸坯质量控制,热送过程控制以及轧后冷却控制密不可分。

Firstly, all the terms concerned are split up into basic term elements-termels, then eight aspects of quantificational indexes are given: errors-in-printing ratio,'inconsistent/uncanonical spelling' ratio,'unnecessary one-many/many-one correspondence' ratio,'inequivalent term' ratio,'discrepant interdisciplinary term' ratio,'unconformable-to-GB term' ratio,'incomplete/redundant term' ratio, and overall 'term worthy of revision/discussion' ratio.

其基本方法,一是从名词集中拆分出基础要素-名词元;二是提出八项量化指标:印误率,英语拼写不一致与不规范率,非必要的一多与多一对应率,英汉名词不对等率,与交叉学科名词有异率,与国标定名不符率,收词欠完备与冗余率及总体值得修榷率。

If by means of a prereduction MRI or after neurologic deterioration during closed reduction, the surgeon becomes aware of a fragment of disc material displaced into the spinal canal, then an anterior discectomy, open reduction, fusion, and plating becomes necessary.2,7,9 In approximately half of the cases, a closed reduction will be successful in reducing the dislocation before surgery.50 In the majority of the others, an intraoperative reduction performed after the discectomy and decompression will achieve anatomic reduction.9,51 For those patients in whom an anterior discectomy and decompression have not been successful in reducing the dislocation, then a supplemental posterior open reduction should be performed.52

假如借助MRI检查,或在闭合复位过程中神经症状进一步加重,外科医生意识到有椎间盘碎片突入了椎管,此时就需要前路椎间盘切除减压、开放复位和固定融合。大约有一半的病例手术以前能够通过闭合复位来成功的将脱位复原,剩下的病例则需要在术中将椎间盘切除减压来达到解剖复位。假如有病人经过前方的椎间盘切除和减压后仍然不能成功的还原脱位,则需要再行后方的开放复位术。

The results show that Fe0.13[Co20Ni80]0.87 alloy fibers are characterized with thin diameters between 0.3 and 2.0 μm, with high aspect ratio, dense and smooth surfaces. The crystalline size of the alloy fibers are mainly influenced by the thermal reduction temperature and are in the range of 20 to 50 nm with a corresponding reduction temperature range of 300 to 700 ℃. The magnetic properties of the alloy fibers are largely affected by the carbon content and crystalline sizes of the alloy fibers. With increasing thermal reduction temperature, the coercivity decreases while the saturation magnetisation value of the alloy fibers dramatically increases at lower reduction temperatures. The alloy fibers prepared at reduction temperature of 700 ℃ have a saturation magnetisation value of 120 Am2/kg and a coercivity value of 10.4 kA/m, respectively.

结果表明:Fe0.13[Co20Ni80]0.87合金纤维的直径为0.3~2.0 μm,表面光滑、长径比大;组成合金纤维的晶粒大小与还原温度密切相关,当温度为300~700 ℃时,晶粒尺寸由约20 nm增加到约50 nm;该合金纤维显铁磁性,其矫顽力主要受合金中C含量及晶粒大小的影响,随制备温度的升高而降低;饱和磁化强度则主要与合金的组分相关,随还原温度的升高和合金纯度的提高而增大;经700 ℃热还原后,合金纤维的饱和磁化强度 m s为120 Am2/kg,矫顽力 H c为10.4 kA/m。

Correctional checking formula of melt flow ratio in injection molding was obtained by introducing a correction coefficient β which reflected the complexity degree of mold cavity. The results show that, the maximum flow ratio of 486 can be obtained when injection pressure ranges from 150 MPa to 160 MPa in Archimedes spiral mold for PP, while maximum flow ratio of 419 can be obtained when injection pressure ranges from 160 MPa to 170 MPa for PE. There is a local fluctuation phenomenon for flow ratio and corresponding injection rate in square spiral mold when injection pressure of 100, 120 and 150 MPa for PP and 130, 140 MPa for PE are reached respectively,and this phenomenon is more serious for good fluidity of melt. The average flow ratio in Archimedes spiral mold is 6% larger than that in square spiral mold for PP, and 4% for PE, the average flow ratio of PP is 19% bigger than PE in Archimedes spiral mold, and 15% in square spiral mold. The influence of the cavity profiles on the melt flow ratio is more significant for good fluidity of melt.

研究结果表明:在阿基米德螺旋线模具中,PP在注射压力为150~160 MPa时取得最大流动比485,PE在注射压力为160~170 MPa时取得最大流动比419;在方形螺旋线模具中,PP在注射压力为100,120和150 MPa,PE在注射压力为130和140 MPa时流动比及所对应的注射速率出现波动,且流动性好的熔体波动更为严重;PP在阿基米德螺旋线模具中的流动比均值较其在方形螺旋线模具中大6%,而PE大4%;在阿基米德螺旋线模具中流动比均值PP比PE的流动比均值大19%,而在方形螺旋线模具中PP的流动比均值比PE的大15%;流动性好的熔体受模具型腔轮廓特征影响大。

NO_x decreasing ratio of micronized coal reburning comparing withgeneral combustion is not proportionable to NO_x reduction ratio in reduction zone,which depends on both NO_x reduction ratio and NO_x increment in burnout zone.

超细粉再燃与常规燃烧相比NO_x脱除率与再燃区NO_x还原率不成正比,它是由NO_x还原率与燃尽区NO_x新的生成综合决定的。

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